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Re: 7603 no trace
Good Day,
Quote: - I'm thinking Q872 and the other 2 transistors are OK.? There's just not quite enough base current to turn on Q872, and the others.? The collector of Q860 is only 2 volts.? It should be about 52V when things are normal (+50V supply + drops of 3 transistors' B-E junctions). Ah, yes - of course - you are raising a good point here Jimmy.? Plus some small drop across R875, of course. Too obvious. I should not try to understand voltage readings and schematics when it's getting late.... David, simply follow Jimmy's advice.? As your - 50V DC voltage reads off, you also might want to check if Q908 is on and Q909 is off during operation. See the description on page 4-30. By the way: I have just seen that Tektronix has followed their own, good tradition and they have use sockets for all small transistors on the 7603's A11 Low Level Regulator board hardware. That should make any potential replacement work or tests easy, if necessary. Cheers, Magnus |
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Total beginner with newly acquired 475 with issues
I am reviving an interest in electronics I had in my youth, my day job is a race car engineer, and I need to get a better grasp of electronics as cars and engine become ever more complex in their management and control strategies. I have bought a bit of basic test gear, as well as stuff I have had for a long time. I now have a working Philips PM3380B analogue / digital scope, a 150 meg USB scope, some basic voltage measurement gear and a basic signal gen. I also have acquired through the ubiquitous Ebay a half dead Tek 475 scope to play with. it cost not a lot and was a surprise win on a bid I put in and forgot about. The abridged story is below:
Right, I picked the 475 up this evening and have had a word with the seller and a quick look inside it. It was stored under far from ideal conditions for some years in an old building undergoing restoration. It has slight signs of this damp on one board, some of the metal canned transistors have the very first signs of green verdigris / corrosion on their cases, very very minor, mind you. One of the vertical side boards has very minor corrosion on some of the ground foil near a vent on the case, but the tracks still appear fine, it's very localised and would clean off I am sure. When the scope was purchased five years ago it worked fine save for the second channel losing the display if turned up to what he described as 2 megs?? Below this ?? it worked fine, and channel one worked fine in all respects. After coming out of storage and being put in a warm dry environment the problems were apparent with which it was sold. It will focus quite well, in the centre of the pot. The dot almost appears to be two very short lines one above the other though, hard to say. Intensity needs to be in the last tenth of clockwise rotation to get any display to show. Horizontal control needs to be fully clockwise to bring the dot to the centre of the screen, a 1/4 or so turn anti clockwise and the dot is off the left of the screen. Beam finder creates a very bright bigger dot, with a lot of illumination on the phosphor around this dot. The vertical control fully clockwise has the dot off the top of the screen, fully anti clock has it a maximum of a 1/4 of the way down. Fiddling with the control will make the display occasionally flash below the vertical half way point instantaneously, as if noise in the pot is doing it. Randomly probing a few of the voltage test points which have their expected voltages shown on the main board give sensible readings, what the ripple is like I have no idea. There's a point marked "5 V unreg" on the main board, this is showing 62.9 volts. Others are within 0.01 volts of the stamped values on a reasonable hand held DMM, referenced to ground tags on the main board. Fan works, three or so of the panel switch plastics are broken, Bezel of main front panel has some corrosion, fascia is so so, but perfectly legible and usable. Would you recommend I attempt more diagnostics, or is the above enough to condemn it as a source of spares only? Thanks. I can post photos. I would like to fix it as it would be my first attempt at fixing anything electrical of any complexity, and very different from working on new automotive engine and chassis control systems. I don't NEED this to work, it won't change my life it it's a white elephant, but I know I'd get a buzz if someone were willing to treat me like a normal Joe passenger who ends up in the cockpit of a plane when the pilot has a seizure and needs talking into landing the thing, however inelegantly ;) All I have are a 150 meg dual channel USB scope, a PM3380B 100 meg dual channel Fluke analogue / digital scope, a bench and a hand DVM, a signal gen that goes only to 1 meg. I have some soldering gear anyone with a true interest in PCB work would probably laugh at, but I don't mind buying a cheap fairly basic soldering un-soldering station, I have fancied something better for years. If I blow it up (further...) I will be annoyed, but would put it down to experience. |
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Re: Tekscopes at the Computer History Museum
--- In TekScopes@..., "phosphorphile" <gumbear@...> wrote:
Another interesting example of analog computer technology was the flight path computer for Nike missiles. The Nike was an early anti-missile system. These were closed loop systems which used radar readings of incoming missiles and the Nike after it was launched. An analog computer computed the trajectory of both and sent information to a telemetry uplink to change the steering vane positions on the missile. This was designed in the early 1960's, and amazingly it actually worked in tests. You can see an example not to far from the Computer history museum in the park directly north of the golden gate bridge ¨C do a Google search to learn more. While analog computers made some amazing advances for their day, I disagree with the comment that they laid the groundwork for modern digital computers. The early designs of digital computers did not leverage anything from analog computers, and took totally independent paths. Probably the only connection is that one of the early digital computers ¨C ENIAC, was designed for the purpose of computing trajectory tables for large field artillery ¨C a similar task the Nike flight path computer performed. The latter provided correction information in real time, while ENIAC actually computed tables of numbers that were published in field manuals. ENIAC had a couple of oscilloscopes stationed near its bays to assist in troubleshooting failed tubes. Some say they were Tek scopes, but I don't think the timing works. ENIAC became fully operational in February 1946 ¨C before Tektronix was founded. - Steve |
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Re: TG501 option 1 connections
Egge Siert
Hi to Both,
I must admit there is something strange with the ribbon connectors used in the TG501A and I think also in the TG501 for the connection of the Multiplier Board to the Main Board. Except the good habit of making good pictures before you disassemble a Module there is a logic in the harmonica(ribbon)connectors. This to compensate for the absence of the notch. Brown is 1, Red is 2. etc. (like the color coding of resistors/capacitors etc.). "Normally" brown is the cable closest to the arrow on the PWB. With the TG501A it is the other way round! 5 is Brown, 4 is Red, 3 is Orange and 2 is Yellow?. I assume with the TG501 it is the same, notwithstanding that the Mainboard is mounted reversed and I cannot clearly see the ribbon between the Multiplier Board and the Main Board in my TG501. I have both thus in case I must.... Egge Siert |
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Re: SOT: Yet another HP 8640b range&peak deviation combination gears lot
On Sun, Jan 22, 2012 at 1:01 PM, Emanuele <emanuele_girlando@...> wrote:
Slightly Off Topic..To save other people the trouble of looking, he charges 16.50 Euros + 11 Euros shipping (to the US), or about $35 total for a gear. Don't know why he doesn't mention that when he posts. |
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Re: Need Manual for Type W, SN 4560 & 5336
Egge Siert
Hi Aaron,
It seems that you have two Type W's with the FET-Frontend and the PWB for these. With SN 7000 and above this was standard. For this late versions a new Manual was printed. FET-Frontends (less drift) were used in late Type 1A1's (I don't for sure also 1A2's) and the 1A7A (which has the same circuit as the later 7A22). Egge Siert |
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Re: SOT: Yet another HP 8640b range&peak deviation combination gears lot
Slightly Off Topic..
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4 more gears available now. Item no 320834621122. Hope this can help. Ciao. Emanuele. --- In TekScopes@..., "Emanuele" <emanuele_girlando@...> wrote:
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Sold: Tek DC510 TM500 Counter (parts or repair)
On 1/22/2012 1:14 PM, Oz-in-DFW wrote:
Unknown, untested, looks to be complete but clearly needs attention.-- mailto:oz@... Oz POB 93167 Southlake, TX 76092 (Near DFW Airport) |
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Re: 7T11 trace shifting left as time/div rotated.
Yes, the measurements ware taken with both the coarse and fine "time position" controls fully clockwise, but that gives me something extra to check on tomorrow.
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Regards, David Partridge -----Original Message-----
From: TekScopes@... [mailto:TekScopes@...] On Behalf Of Albert Sent: 22 January 2012 16:33 To: TekScopes@... Subject: [TekScopes] Re: 7T11 trace shifting left as time/div rotated. Hi David, The start and stop levels should differ about 5 V. With start I (and you also I think) actually mean the stop level when the trace is at the left position. On the test scope you look at vertical position of the horizontal lines. It depends of Time Position. The graph 11 is for fully CW. If you rotate to fully CCW then the whole patter shift 5 V lower, from -5 V to -10 V. Albert
------------------------------------ Yahoo! Groups Links |
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Re: Power supply problem with Tek 2220
Mark Wendt (Contractor)
Got a temperature controlled desoldering station with an air pump?
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Mark On 1/22/2012 11:14 AM, Tan Chor Ming wrote:
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FS: Tek DC510 TM500 Counter (parts or repair)
Unknown, untested, looks to be complete but clearly needs attention.
Known issues: INST ID button is sticky Missing a side cover CHANNEL B BNC out of round, but looks reshapeable. ARM SMB is damaged and will need to be replaced. High Res pics at $50 or best offer +$15 shipping in US. International shipping is available, but you'll cover all costs, fees, and tariffs. -- mailto:oz@... Oz POB 93167 Southlake, TX 76092 (Near DFW Airport) |
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Re: Need Manual for Type W, SN 4560 & 5336
¿ªÔÆÌåÓýAaron;
I believe you may be?looking at a "W" with the front-end mod kit
installed.
I have several "W"s and an NIB mod kit.
Will have to go diggin' though...
Bernd Schroder
?
In a message dated 1/22/2012 2:27:20 A.M. Pacific Standard Time,
ataylor@... writes:
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Full-time opening for a community leader for oscilloscope site
Hi there,
I'm looking for a creative engineer/writer/community leader with some hands-on 'scope experience to run an online community focused on the use and application of that most critical of engineers?€? tools, the oscilloscope. Day-to-day responsibilities include one or two blogs and recruiting and managing other paid bloggers to do likewise, again with an emphasis on test issues and how scopes can be used to solve them, but with latitude to explore the life and daily issues designers face. Position is full-time with competitive compensation, extensive benefits and broad exposure in the industry. Some travel may be required, for training and a couple of industry shows per year, but otherwise it?€?s a work-from-home (or wherever you prefer to work) position. If ou like scopes, and you're interested, let me know at patrick.mannion@.... |
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Re: Tekscopes at the Computer History Museum
Bernice Loui
--- On Sun, 1/22/12, phosphorphile wrote:
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Re: Power supply problem with Tek 2220
Oh my, I see another long discussion starting :).
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I think that when a high ESR is seen, most of the time, the capacitance falls. At least that is my observation. But also, the power dissipated is proportional to ESR and square law to (V)oltage (E^2). Anyway, hot capacitors are not normal in my experience. Anyone else care to comment? Regards, Tom M ----- Original Message -----
From: Tan Chor Ming To: TekScopes@... Sent: Sunday, January 22, 2012 12:00 PM Subject: RE: [TekScopes] Re: Power supply problem with Tek 2220 Hello Tom, You are right, high ESR will have high ripple. But heat on cap = (V ripple rms)* (V ripple rms) / ESR (V ripple rms) depends on the capacitance. Higher capacitance ¨¤ less ripple Without the ESR being low there will be less heat This is what I thought, I stand corrected. Rgds, Chor Ming ------------------------------------------------------------------------------ From: TekScopes@... [mailto:TekScopes@...] On Behalf Of Thomas Miller Sent: Monday, January 23, 2012 12:35 AM To: TekScopes@... Subject: Re: [TekScopes] Re: Power supply problem with Tek 2220 Hello Tan, You say: "The filtering caps are also warm (quite hot) which means that it is filtering the ripple and converting to heat. It's not an indication of good ESR though but poor ESR will have less heat. I do not suspect the caps causing the shutdown issue. As an improvement, I may change it later but not now, unless I am convince that poor ESR can cause shutdown. A high ESR will make the capacitor run hot because of the higher ripple voltage. If you detect a hot capacitor, you should replace it with a known good cap. You might just try tacking a good cap across the suspect cap to confirm the problem. Regards, Tom ----- Original Message ----- From: Tan Chor Ming To: TekScopes@... Sent: Sunday, January 22, 2012 11:07 AM Subject: RE: [TekScopes] Re: Power supply problem with Tek 2220 Ed, Thank you for your extensive reply. 2220 is a storage 60mHz 2235 is a 100Mhz Non-storage The power supply of the 2220 is quite similar to the 2235 which I can see from the layout. These are some differences on the power supply 1.. 2220 has an additional -5V supply 2.. Current rating in at the 43V for 2220 is higher. Based on design, R912 is 357 ohm for 2235 and 549 ohm for 2220. This means current limit for 2235 = 0.86A and for 2220 = 1.3A 3.. The added current is needed to drive the digital storage function which is a separate board 4.. Based on calculation, Shutdown voltage at R907 for 2235 = 0.18V and for 2220 = 0.26V. Measured value on 2220 is .285V. I have a DMM, Analog Multimeter and my other scope a 2235 has also a failed SCR for the crowbar. I did not want to fire it up until I get the crowbar function fixed. I am planning to get an isolation transformer and run it at 110, before I use my other scope if it is fixed to measure the signal of the 2220. This is the development so far. I have changed the following C925, C943, C942, C940 with little improvement I have also remove the connector to Q9070 and solder it directly to the leads. This seems to have the most improvement Lifted the +5V supply to the digital board Measured voltage on R907 at cold state = 0.17V (about 0.85A on 43V) Measured voltage on R907 in warm state (after 5 mins) = 0.19V (about 0.95A on 43V) Scope can sustain operation for more than 15 minutes before the supply shutdown and up again for another 5~10 min and repeat. This shows an intermittent overload condition. Not that bad because the scope can be used with brief shutdown in-between. Connect the +5V to the digital board Measured voltage on R907 at cold state = 0.22V (about 1.1A on 43V) Measured voltage on R907 in warm state (after 1 mins) = 0.25V (about 1.25A on 43V) Scope can sustain operation for more than 1 minutes before the supply shutdown and up again repeat every seconds later. This shows a sustained overload condition. Measured voltage on pin15 of U930 is 0.285, Clearly, the overload should not happen since this voltage limit for voltage at R907 before shutdown happens. This confirms that there are spike signal riding on R907 that cause the comparator in U930 to cause a shutdown. 20Khz test I thought maybe the pre-regular was running at slightly higher frequency causing the switching efficiency to drop which cause Q9070 and T906 to heat up. Since I do have a working scope, I found an interesting way to test this without instrument. 1.. Connect a 470pf across C919 and the frequency will drop to ~15Khz because I can heard the switch buzz. 2.. Without the 470of, I could not heard the switching buzz, so I knew it must be slightly past 20Khz 3.. I confirm this because my son is able to hear the 20Khz buzz. ESR on Cap. I tried to change caps on C960 and C961, but there is no change to the behaviour and leakage current on removed caps seems to be low, so I do not suspect it is a ESR on cap issue. The filtering caps are also warm (quite hot) which means that it is filtering the ripple and converting to heat. It's not an indication of good ESR though but poor ESR will have less heat. I do not suspect the caps causing the shutdown issue. As an improvement, I may change it later but not now, unless I am convince that poor ESR can cause shutdown. I am very much back to square one, because everything seems to point to a normal working scope except that heat generated has cause an overload condition What's next. 1. Poor Switching I suspect that there is a poor switching from Q9070 and CR907 which can cause Q9070 to heat up in forward inverter. Haven't gotten the component so will have to explore this later. Q9070 (P6N55) needs to be at least 600V, 6A, RDSon 1.5 ohm CR907 (BDY73G) needs to at least 600V, 1A, Reverse recovery time 50nS. Need 2 of these for 2220 in parallel, I believe 2235 uses only one. . 2.. Overload This is a likelihood but I need a reference to know if the current measure on +43V is too high. How could power ESR cause overload? Poor ESR will cause poor functional performance because there is high ripple on the DC but will it cause an overload? Background. Both scope were working scope which I have not used for more than a year Final Action if all else fails. I am quite sure if I run the 2220 at 110V the shutdown issue will go away because of lower generated heat with 110V. If the problem persist, I will just have to switch to a lower line voltage supply on an isolation transformer. Rgds, Chor Ming ---------------------------------------------------------------------------- From: TekScopes@... [mailto:TekScopes@...] On Behalf Of Ed Breya Sent: Sunday, January 22, 2012 2:43 AM To: TekScopes@... Subject: [TekScopes] Re: Power supply problem with Tek 2220 Yes indeed, the 2220 is virtually identical to the 2230 in most respects - just a notch down to fill the price v. performance market position at the time. The 2200 series models share the same basic power supply topology, tweaked to get more power for the digital storage add-ons. Your equipment appears to be very limited, but you do have a working DMM and a "working" scope available for a few minutes at a time. You can use it to look at its own supplies and other circuitry, at least up to the point of shutdown. Before delving further into the supply, I recommend that you first check your line voltage to see if it's on the high side, or possibly has transients or surges that may be causing the scopes to self-protect. I don't recall if the 2220 has the "trigger view" feature, but if so, set up for line triggering, and activate that to see roughly what the line looks like. This is band limited, so won't show fast transients. You can also look at the line voltage directly and more accurately with a X10 probe tip to the hot side. DO NOT connect the ground clip to anything, or preferably, disconnect it from the probe whenever poking around line voltage. As I recall, the scopes should run on any line voltage between the specified limits, with no range switching needed. If you have access to a variac or step-down transformer you can try running at lower line voltage. If not, you can try loading down the branch circuit with extra lighting and appliances to see if it drops significantly, or even try something wired temporarily in series, like a space heater, coffee pot, or a large incandescent lamp. Some background info should help: 1. Were these scopes working and then stopped, or did you just get them, and they didn't work? It seems from your initial post that they both failed at the same time. If so, one big thing in common would be line voltage problems. Do both scopes exhibit the same symptoms? 2. Is the available run time always about the same before shutting down? Does recycling the power make it run for the same length of time, or does it need to cool down first? If the shutdown timing is fairly predictable, it may be good to monitor the outputs closely and watch to see if they sag or rise just before shutdown. Also, watch the display closely for dimming or blooming - evidence of same on the high voltage. Also, look at the 20 kHz AC waveforms on the secondaries, ahead of the output rectifiers to see if they are nice, rounded squarish waves, and see if that shape changes just before shutdown. That's probably enough for now. I agree with the suggestion to revisit the 2235. It may be easier to fix, or you may luck out and find it's problem - then you'll have one fully working scope - a big improvement. Ed --- In TekScopes@..., David <davidwhess@...> wrote: > > When I was searching for a replacement channel swtich, I found that a > number of the 22xx series oscilloscopes have the same main board which > has the power supply including the 2213A, 2215A, 2230, 2232, 2235, > 2236 but not the 2213 or 2215. For the analog only models, the extra > outputs which would go to the digital storage board are tied to ground > to maintain bias on the channel switches. The 2220 is much rarer with > no online service manual so I never checked it. > > On Sat, 21 Jan 2012 06:28:59 -0800, "tom jobe" <tomjobe@...> > wrote: > > >Hi Tan, > >Some one told me that the 2220 is the 60 MHz version of the 2230 100 MHz > >scope. If this is true, the 2230 manual might be your best bet. It is > >available from several places including: > > > > > > > >Now that I hear about your experience level and what equipment you have on > >hand, I would fix the 2235 first as it has no top board limiting your access > >to the power supply (and almost everything else in the scope) while the > >scope is actually running. > > > >You mention the need for an isolation transformer. You probably do not need > >an isolation transformer at this point, as its only value is to be able to > >"float" the scope so you can use another scope to look at the inverter side > >of the power supply. The inverter is already making the 43 VDC so what would > >you need to check anyway? I know the service manual calls for an isolation > >transformer (so I bought one) but my experience finds it to be fairly > >useless in the 22xx repair process. Also, once you "float" the scope the > >chassis of the scope is now at some elevated voltage, which is a little > >scary for an amateur like me. > > > >You mentioned that Q908 was up on the heatsink but it isn't. Take a closer > >look as it only is involved in running the "gate" of Q9070. > >Q9070 is up on the heatsink. Q908 is a small transistor with minor currents > >through it, and Q9070 does the real work of creating the 43 VDC for the > >inverter. > > > >If you ever decide to do the external injection of the 43 VDC, you need to > >disconnect Q9070, not Q908. > >tom jobe... > > > > > > > > > > > > > > > > > > > >----- Original Message ----- > >From: "Tan Chor Ming" <jonray03@...> > >To: <TekScopes@...> > >Sent: Friday, January 20, 2012 8:37 PM > >Subject: RE: [TekScopes] Power supply problem with Tek 2220 > > > > > >> Thank you Tom for taking the time to point out specifically the likely > >cause > >> of the problem. > >> > >> I know it takes effort to go through the details and I really appreciate > >it. > >> > >> > >> > >> Just to let you know where I come from, so that there is less to assume. > >> > >> I am an electronics engineer from Singapore above 50 so very much familiar > >> with vacuum and solid state electronics. > >> > >> I do not have the schematics for 2220 so like you I am assuming it is > >quite > >> similar to 2235 which I have it downloaded. > >> > >> I have both 2220 and 2235 and there appear to be quite similar though the > >> PCB layout is slightly different. > >> > >> I have complete understanding of how the power supply works. > >> > >> Pre-regulator - PWM driving Q908 to produce +43V across TP940 and TP950 > >> > >> Final Regulator - DC-DC push-pull inverter through Q947 and Q946. > >> > >> > >> > >> I have another scope 2235, unfortunately, it too went down at the same > >time, > >> so the only instrument I have is a multimeter. > >> > >> Anyway, I do not have an isolation transformer so even with the 2235 > >> working, I will need to get an isolation transformer before I could take > >any > >> measurement. > >> > >> Any idea what VA rating is needed for the isolation transformer? > >> > >> Based on the power needs, it appears to be at least 200VA. > >> > >> > >> > >> Initially, I was asking about R907, not because I was suspecting the > >> resistor but I intend to check the load current by putting an ammeter in > >> series with the resistor. > >> > >> For that to be useful I need to know what is expected. Like you. I am > >> suspecting that the voltage at R907 has gone up after the set warms up > >thus > >> shutting down U930. > >> > >> > >> > >> I will probably go with the cap changes you have recommended since I have > >> some time during the Lunar New Year break. > >> > >> Unfortunately, I do not have ESR meter, but I don't think that a big issue > >> just replacing the caps. > >> > >> > >> > >> I am aware of the direct 43Vdc injection, but thank you for telling me the > >> detail that Q908 needs to be disconnected. > >> > >> Unfortunately, I do not have a power supply with this voltage output. I > >> only have a power supply of 18V max 2A. So I will have to hold off this > >> approach. > >> > >> > >> > >> One more thing which I did not mention earlier is that I detached the > >+5.2V > >> connection to the digital board (for the storage function of 2220) and > >> behaviour remains unchanged. > >> > >> > >> > >> Rgds, > >> > >> Chor Ming > >> > >> _____ > >> > >> From: TekScopes@... [mailto:TekScopes@...] On > >Behalf > >> Of tom jobe > >> Sent: Saturday, January 21, 2012 7:30 AM > >> To: TekScopes > >> Subject: Re: [TekScopes] Power supply problem with Tek 2220 > >> > >> > >> > >> > >> > >> I saw your 2220 question the first time you posted it a few days ago, and > >I > >> did not have a nice short answer for you. Since you have not gotten the > >> answer > >> you were looking for, let me comment a bit on this. > >> First off, I don't own a 2220 or have the service manual for it, and none > >of > >> the download sites I checked seem to have it either, including > >> ArtekMedia.com having it for purchase. So I will assume it is similar to > >the > >> better 22xx's such as the 2235, at least around the power supply. I will > >> also assume that you do have a service manual to work with. U930 monitors > >> the voltage drop across R907, and in your case it probably thinks the > >> current is too high after a few minutes, so it shuts down. > >> I have worked on lots of 22xx scopes and I have not seen the value of R907 > >> drift and cause this problem, but others have reported that as a > >> possibility. Odds are, that this is not your problem. > >> An over current situation can be caused by anything after R907 within the > >> inverter, the transformer itself or on the secondary side of the main > >> transformer. > >> How you go about finding the problem depends on what equipment you have > >> available, and what your testing preferences might be. > >> If you don't have much to work with, just start changing components. In my > >> experience the components in the right rear corner of the mainboard cause > >> the most grief so I would start there with C925, C942 and C943. If you > >have > >> some decent soldering equipment you can change all three capacitors > >quickly > >> without removing the mainboard. > >> If you have access to an ESR meter you could check all of the aluminum > >> electrolytic capacitors in circuit. Most of the electrolytics give no > >> trouble, especially the six(?) 840 uF caps in front of the heat sink for > >> Q9070 (but you would want to check all of the electrolytic caps if you had > >> an ESR meter handy). > >> Another approach would be to put in the 43 volts DC from an external power > >> source until something got hot or went up in smoke. If your power supply > >> allowed you to adjust the current limit you could sneak up on it and just > >> get the problem part(s) nice and warm. You will need to at least > >disconnect > >> Q9070 when you apply the external 43 VDC at TP940 and TP 950 from the > >bottom > >> or top of the mainboard. I lightly tack on two wires to the bottom side to > >> make the 43 VDC connections. You can use the scope in its normal way when > >it > >> is powered with the external 43 VDC. > >> The external 43 VDC idea came from a fine Tekscopes member named Hakan, > >many > >> years ago, and he has an excellent document you should read at: > >> > >> A couple of years ago I made up a document listing some commonly available > >> components you might use to replace some of the original Tektronix part > >> numbers that often fail. I can send you that directly or you can find it > >in > >> the Tekscopes Message archive if you like. > >> Another thing you might do is take resistance readings from chassis ground > >> to each of the voltage test points before you get very far into this > >repair > >> (with the scope not connected to the mains of course!). > >> There are lots of other ideas to add to this, but this should get you > >> started. > >> This will be a simple fix, so just take your time and understand what you > >> are doing. > >> tom jobe... > >> > >> ----- Original Message ----- > >> From: "Tan Chor Ming" <jonray03@... > >> <mailto:jonray03%40singnet.com.sg> > > >> To: <TekScopes@... <mailto:TekScopes%40yahoogroups.com> > > >> Sent: Friday, January 20, 2012 6:45 AM > >> Subject: Re: [TekScopes] Power supply problem with Tek 2220 > >> > >> > Has anyone seen this behaviour repairing Tek2000 series scope power > >> supply? > >> > > >> > > >> > > >> > Behaviour > >> > > >> > 1. When power on from cold, it will fire up properly and stay on for a > >few > >> > minutes > >> > > >> > 2. Once it warms up, the power supply shut down and try to on again and > >> it > >> > continues in this on/off mode > >> > > >> > 3. Pre-regulator out = 43V (between TP940 and TP950) > >> > > >> > 4. All voltages when the unit is stable for a few minutes are > >+8.6, -8.6, > >> > +5.2, +100 are all ok. > >> > > >> > > >> > > >> > What are likely problems before I start ripping the components from the > >> > circuit? > >> > > >> > > >> > > >> > ttesenq@... <mailto:ttesenq%40tiscali.co.uk> suggested that > >it > >> could be the pre-regulator MOSFET > >> > P9070. > >> > > >> > > >> > > >> > I though that it could be a electrolytic cap but it doe not look likely > >> > because electrolytic failure would not have allowed the unit to fire up > >> for > >> > a few minutes > >> > > >> > It is more likely a active component that weaken with increase > >> temperature, > >> > so ttesenq@... <mailto:ttesenq%40tiscali.co.uk> could be > >right. > >> > > >> > This would mean Q947 and Q946 are also likely components > >> > > >> > > >> > > >> > Any other possible lead of similar experience. > >> > > >> > > >> > >> > >> > >> > |
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Re: Tekscopes at the Computer History Museum
In the Navy in '65 I was treated to a visit inside an F4 Phantom simulator trailor. That was one big analog electromechanical maise on wheels. Analog computers laid the ground work for digital to take off from.
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......They have heard of analog computers, sort of, but they're treated like the redheaded stepchild. ....... |
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Re: Power supply problem with Tek 2220
Tan Chor Ming
Hello Tom,
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You are right, high ESR will have high ripple. But heat on cap = (V ripple rms)* (V ripple rms) / ESR (V ripple rms) depends on the capacitance. Higher capacitance --> less ripple Without the ESR being low there will be less heat This is what I thought, I stand corrected. Rgds, Chor Ming _____ From: TekScopes@... [mailto:TekScopes@...] On Behalf Of Thomas Miller Sent: Monday, January 23, 2012 12:35 AM To: TekScopes@... Subject: Re: [TekScopes] Re: Power supply problem with Tek 2220 Hello Tan, You say: "The filtering caps are also warm (quite hot) which means that it is filtering the ripple and converting to heat. It's not an indication of good ESR though but poor ESR will have less heat. I do not suspect the caps causing the shutdown issue. As an improvement, I may change it later but not now, unless I am convince that poor ESR can cause shutdown. A high ESR will make the capacitor run hot because of the higher ripple voltage. If you detect a hot capacitor, you should replace it with a known good cap. You might just try tacking a good cap across the suspect cap to confirm the problem. Regards, Tom ----- Original Message -----
From: Tan Chor <mailto:jonray03@...> Ming To: TekScopes@... Sent: Sunday, January 22, 2012 11:07 AM Subject: RE: [TekScopes] Re: Power supply problem with Tek 2220 Ed, Thank you for your extensive reply. 2220 is a storage 60mHz 2235 is a 100Mhz Non-storage The power supply of the 2220 is quite similar to the 2235 which I can see from the layout. These are some differences on the power supply 1. 2220 has an additional -5V supply 2. Current rating in at the 43V for 2220 is higher. Based on design, R912 is 357 ohm for 2235 and 549 ohm for 2220. This means current limit for 2235 = 0.86A and for 2220 = 1.3A 3. The added current is needed to drive the digital storage function which is a separate board 4. Based on calculation, Shutdown voltage at R907 for 2235 = 0.18V and for 2220 = 0.26V. Measured value on 2220 is .285V. I have a DMM, Analog Multimeter and my other scope a 2235 has also a failed SCR for the crowbar. I did not want to fire it up until I get the crowbar function fixed. I am planning to get an isolation transformer and run it at 110, before I use my other scope if it is fixed to measure the signal of the 2220. This is the development so far. I have changed the following C925, C943, C942, C940 with little improvement I have also remove the connector to Q9070 and solder it directly to the leads. This seems to have the most improvement Lifted the +5V supply to the digital board Measured voltage on R907 at cold state = 0.17V (about 0.85A on 43V) Measured voltage on R907 in warm state (after 5 mins) = 0.19V (about 0.95A on 43V) Scope can sustain operation for more than 15 minutes before the supply shutdown and up again for another 5~10 min and repeat. This shows an intermittent overload condition. Not that bad because the scope can be used with brief shutdown in-between. Connect the +5V to the digital board Measured voltage on R907 at cold state = 0.22V (about 1.1A on 43V) Measured voltage on R907 in warm state (after 1 mins) = 0.25V (about 1.25A on 43V) Scope can sustain operation for more than 1 minutes before the supply shutdown and up again repeat every seconds later. This shows a sustained overload condition. Measured voltage on pin15 of U930 is 0.285, Clearly, the overload should not happen since this voltage limit for voltage at R907 before shutdown happens. This confirms that there are spike signal riding on R907 that cause the comparator in U930 to cause a shutdown. 20Khz test I thought maybe the pre-regular was running at slightly higher frequency causing the switching efficiency to drop which cause Q9070 and T906 to heat up. Since I do have a working scope, I found an interesting way to test this without instrument. 1. Connect a 470pf across C919 and the frequency will drop to ~15Khz because I can heard the switch buzz. 2. Without the 470of, I could not heard the switching buzz, so I knew it must be slightly past 20Khz 3. I confirm this because my son is able to hear the 20Khz buzz. ESR on Cap. I tried to change caps on C960 and C961, but there is no change to the behaviour and leakage current on removed caps seems to be low, so I do not suspect it is a ESR on cap issue. The filtering caps are also warm (quite hot) which means that it is filtering the ripple and converting to heat. It's not an indication of good ESR though but poor ESR will have less heat. I do not suspect the caps causing the shutdown issue. As an improvement, I may change it later but not now, unless I am convince that poor ESR can cause shutdown. I am very much back to square one, because everything seems to point to a normal working scope except that heat generated has cause an overload condition What's next. 1. Poor Switching I suspect that there is a poor switching from Q9070 and CR907 which can cause Q9070 to heat up in forward inverter. Haven't gotten the component so will have to explore this later. Q9070 (P6N55) needs to be at least 600V, 6A, RDSon 1.5 ohm CR907 (BDY73G) needs to at least 600V, 1A, Reverse recovery time 50nS. Need 2 of these for 2220 in parallel, I believe 2235 uses only one. . 2. Overload This is a likelihood but I need a reference to know if the current measure on +43V is too high. How could power ESR cause overload? Poor ESR will cause poor functional performance because there is high ripple on the DC but will it cause an overload? Background. Both scope were working scope which I have not used for more than a year Final Action if all else fails. I am quite sure if I run the 2220 at 110V the shutdown issue will go away because of lower generated heat with 110V. If the problem persist, I will just have to switch to a lower line voltage supply on an isolation transformer. Rgds, Chor Ming _____ From: TekScopes@... [mailto:TekScopes@...] On Behalf Of Ed Breya Sent: Sunday, January 22, 2012 2:43 AM To: TekScopes@... Subject: [TekScopes] Re: Power supply problem with Tek 2220 Yes indeed, the 2220 is virtually identical to the 2230 in most respects - just a notch down to fill the price v. performance market position at the time. The 2200 series models share the same basic power supply topology, tweaked to get more power for the digital storage add-ons. Your equipment appears to be very limited, but you do have a working DMM and a "working" scope available for a few minutes at a time. You can use it to look at its own supplies and other circuitry, at least up to the point of shutdown. Before delving further into the supply, I recommend that you first check your line voltage to see if it's on the high side, or possibly has transients or surges that may be causing the scopes to self-protect. I don't recall if the 2220 has the "trigger view" feature, but if so, set up for line triggering, and activate that to see roughly what the line looks like. This is band limited, so won't show fast transients. You can also look at the line voltage directly and more accurately with a X10 probe tip to the hot side. DO NOT connect the ground clip to anything, or preferably, disconnect it from the probe whenever poking around line voltage. As I recall, the scopes should run on any line voltage between the specified limits, with no range switching needed. If you have access to a variac or step-down transformer you can try running at lower line voltage. If not, you can try loading down the branch circuit with extra lighting and appliances to see if it drops significantly, or even try something wired temporarily in series, like a space heater, coffee pot, or a large incandescent lamp. Some background info should help: 1. Were these scopes working and then stopped, or did you just get them, and they didn't work? It seems from your initial post that they both failed at the same time. If so, one big thing in common would be line voltage problems. Do both scopes exhibit the same symptoms? 2. Is the available run time always about the same before shutting down? Does recycling the power make it run for the same length of time, or does it need to cool down first? If the shutdown timing is fairly predictable, it may be good to monitor the outputs closely and watch to see if they sag or rise just before shutdown. Also, watch the display closely for dimming or blooming - evidence of same on the high voltage. Also, look at the 20 kHz AC waveforms on the secondaries, ahead of the output rectifiers to see if they are nice, rounded squarish waves, and see if that shape changes just before shutdown. That's probably enough for now. I agree with the suggestion to revisit the 2235. It may be easier to fix, or you may luck out and find it's problem - then you'll have one fully working scope - a big improvement. Ed --- In TekScopes@... <mailto:TekScopes%40yahoogroups.com> , David <davidwhess@...> wrote: on accesshand, I would fix the 2235 first as it has no top board limiting your needto the power supply (and almost everything else in the scope) while the toan isolation transformer at this point, as its only value is to be able side"float" the scope so you can use another scope to look at the inverter wouldof the power supply. The inverter is already making the 43 VDC so what isolationyou need to check anyway? I know the service manual calls for an closertransformer (so I bought one) but my experience finds it to be fairly currentslook as it only is involved in running the "gate" of Q9070. tothrough it, and Q9070 does the real work of creating the 43 VDC for the appreciatedisconnect Q9070, not Q908. assume.it. familiar thewith vacuum and solid state electronics.quite takePCB layout is slightly different.time, inanymeasurement. haveseries with the resistor.thus issuesome time during the Lunar New Year break. thejust replacing the caps. [mailto:TekScopes@... <mailto:TekScopes%40yahoogroups.com> ] Ondetail that Q908 needs to be disconnected.+5.2V andBehalfOf tom jobe noneIdid not have a nice short answer for you. Since you have not gotten the toofthe download sites I checked seem to have it either, including willthebetter 22xx's such as the 2235, at least around the power supply. I monitorsalso assume that you do have a service manual to work with. U930 R907the voltage drop across R907, and in your case it probably thinks the thedrift and cause this problem, but others have reported that as a myinverter, the transformer itself or on the secondary side of the main causeexperience the components in the right rear corner of the mainboard forthe most grief so I would start there with C925, C942 and C943. If youhavesome decent soldering equipment you can change all three capacitorsquicklywithout removing the mainboard. hadQ9070 (but you would want to check all of the electrolytic caps if you poweran ESR meter handy). supplysource until something got hot or went up in smoke. If your power justallowed you to adjust the current limit you could sneak up on it and toget the problem part(s) nice and warm. You will need to at leastdisconnectQ9070 when you apply the external 43 VDC at TP940 and TP 950 from thebottomor top of the mainboard. I lightly tack on two wires to the bottom side whenmake the 43 VDC connections. You can use the scope in its normal way availableitis powered with the external 43 VDC.many itcomponents you might use to replace some of the original Tektronix part groundinthe Tekscopes Message archive if you like. youto each of the voltage test points before you get very far into thisrepair(with the scope not connected to the mains of course!). <mailto:TekScopes%40yahoogroups.com> >are doing. aSent: Friday, January 20, 2012 6:45 AM andfewminutes theit+8.6, -8.6,continues in this on/off mode likelyitcircuit? upbecause electrolytic failure would not have allowed the unit to fire forright.a few minutestemperature, |
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Re: Power supply problem with Tek 2220
¿ªÔÆÌåÓýHello Tan,
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You say:
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"The filtering caps are also warm (quite hot) which means that it is filtering the ripple and converting to heat.? It¡¯s not an indication of good ESR though but poor ESR will have less heat.? I do not suspect the caps causing the shutdown issue.? As an improvement, I may change it later but not now, unless I am convince that poor ESR can cause shutdown. ?
A high ESR will make the capacitor run hot because of the higher ripple
voltage. If you detect a hot capacitor, you should replace it with a known good
cap. You might just try tacking a good cap across the suspect cap to confirm the
problem.
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Regards,
Tom
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