From:[email protected] <[email protected]> On Behalf Of Dr. David Kirkby, Kirkby Microwave Ltd Sent: 15 August 2022 10:09 To:[email protected] Subject: Re: [Test Equipment Design & Construction] Boonton Q Meter Thermocouple & Precision Resistor
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On Sun, Aug 14, 2022 at 08:31 AM, Chuck Moore wrote:
The question was asked previously why the thermcouple heads in the Boonton Q Meters were so fragile and prone to burnout so easily.
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If you look at:
That's Brooke Clarke, who is a member of this list.
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Back to the Q Meter.
The thermocouple is heated by a short length of what is reported to be nichrome wire. The writer at prc68 reports the wire is 37 gauge or 0.0045" in diameter. The nichrome wire heater and the thermocouple both are mounted on the bakelight disc inside the sensor head. and the thermocouple bead is welded to the heater wire.
In looking at a chart which showed various nichrome wire gauges and the expected temperature of the wire when a specified current flows through the wire, 37 gauge Nichrome A wire would reach 1600 degrees F for 1000 milliAmps flowing through the wire.
Looking at the chart found here:
you can see a fairly wide range of temperatures for currents varying from 350 milliAmps (400 degrees) to 1290 milliAmps (2000 degrees F). The reported melting point for Nichrome A wire is 2,552 degrees F. The current to reach 2000 degrees is only 29% over the current reported to be flowing in the precision resistor in the Q Meter.
Ah, so the sense wire gets very hot. I assume that means ambient temperature changes are no so significant, as it's so far above ambient.
I thought I read in the 260-A manual that the RF signal generator only run at 50% of the power that could destroy the thermocouple, implying this would not happen like it did in the 160-A But maybe I got that wrong.
If you examine the scale of Boonton 260's Multiply Meter which is monitoring the current through the nichrome wire, the meter is marked with a red zone that begins at about 5% of the meter scale above the meter scale's "Multiply by 1" mark. It appears that the heater operates at a temperature that is was approaching 63% of the wire's melting point.
Em, I like to design things with a bit more to spare than that!
Peter Olin, AI2V (reported to be a silent key) at one time provided repairs and conversions of the 260 Q meter to include sensor head repairs. I also remember that one conversion of the unit led to the vacuum tubes being replaced with solid state active devices. From what I could determine most conversions were driven by the lack of availability of the BR535 vacuum tube (triode) used in the integral AC VTVM.? (I will repeat what I stated pre- viously, the BR535 was a hand selected triode. A popular triode of the period (I forget the industry part number for the tube) was purchased by Boonton and each tube was tested for use in the Q Meter. Peter told me that culling was dictated by an abrupt change in input impedance of the tube at 1 MHz. Apparently there was a relatively frequent production error in manufacturing the tube that caused the perturbation and Boonton's solution was to cull tubes which presented with the undesired characteristic.
Another piece of information from my notes on the box is the resistors R203 and R204 in the leads to the "Multiply by" meter are hand picked at the time of installation of the thermocouple head. Apparently the output voltage slope of the thermcouples varied and to compensate for the delta between units, the resistor values were adjusted. Values generally were between 30 ohm and 65 ohm. Equal value resistors were used in each lead. The capacitors were in place to attenuate RF that might couple into the sensitive "Multiply by" meter. The typical 0.01 uF value was chosen for service.
Many of the older units have a General Electric voltage stablilizer block mounted on the floor of the box. In the last 20 years each one I encountered either had failed or was in the process of failing. The devices are enclosed in a stamped metal shell and filled with a 'GOO' that makes a mess when the unit overheats. The GE boxes were there to address line voltage fluctuations. Given the stench they made when going up in smoke, I pulled the stabilizers out and use an external UPS to provide well regulated AC power.
Please let me know if you notice any of the above info is in error and also of any additions you might make.
Regards
Chuck WD4HXG
Thank you. Your comments certainly help understand why the things burn out so easily.
How does one know if the thermocouple assembly is faulty? I ask this from the view of a person that has bought a supposedly working 160-A from eBay from a seller with a rather poor feedback. The attraction to the auction was the unit appears in good physical shape and that the shipping charges were less than $30 from the USA to the UK. I don't yet have the meter, but would like to know how to run some checks when it arrives. I do have a couple of Boonton Q standard inductors. One covers 50 kHz to 150 kHz and the other 150 kHz to 450 kHz.