On Sun, Sep 22, 2019 at 4:16 PM Brendan Smith <brenatlilydale@...> wrote:
[Edited Message Follows]
It¡¯s quote possible the motor is slightly bad for whatever reason.? Try swapping motors Ra to Dec etc
the reason it¡¯s bad at sidereal (I¡¯m assuming it¡¯s a G1) is the motor drive energy delivered is low.? At higher drive rates it¡¯s provided with more energy....it moves faster. it could be a bad ¡°H¡± bridge but I doubt it.? So try swap the motors over.?
If the system is a G2, you can enter the WEB interface and select¡±servos¡± page:
In this you can increase the servo motor tracking percentage ( increase energy) to the motor.? Try increasing it a little let¡¯s say 35%
it could also be as Michael said or a slipping motor pinion gear