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X Air Hanuman: engine-out


 

Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


 

开云体育

My only concern is “slamming” the throttle …..

It is ok to aggressively pull the throttle back to idle when recovering from , for example, a spiral dive, ?but I would never “slam “ it back. ??
No idea if that gad any bearing on your problem.?

At other times throttle should be advanced or retarded more gradually …..

Regards, ?

Geoff Gartshore
Zenith CH200 GCUD
Waterloo, Ontario?

On Apr 30, 2022, at 5:48 PM, Justin Gregoris <jgregoris789@...> wrote:

?Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


 

?
I suspect it was carb ice, the first Jabiru powered std xair I built used to stop everytime when you closed the throttle on approach once we installed carb heat it sorted it out.
Seamus

----- Original Message -----
Sent: Saturday, April 30, 2022 10:48 PM
Subject: [XAIR] X Air Hanuman: engine-out

Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


 

开云体育

Carb ice??

I was flying 1000AGL, 17 celsius, 8knot wind from the east. Not exactly sure what the humidity was.

I have electronic carb heat but that was not on at any point throughout the flight.



From: [email protected] <[email protected]> on behalf of Seamus O'Donnell <etronics@...>
Sent: Saturday, April 30, 2022 7:11:33 PM
To: [email protected] <[email protected]>
Subject: Re: [XAIR] X Air Hanuman: engine-out
?
I suspect it was carb ice, the first Jabiru powered std xair I built used to stop everytime when you closed the throttle on approach once we installed carb heat it sorted it out.
Seamus
----- Original Message -----
Sent: Saturday, April 30, 2022 10:48 PM
Subject: [XAIR] X Air Hanuman: engine-out

Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


 

开云体育

Many years ago, we had a series of engine stoppages with an early Jab.? We tried all manner of tricks to prevent carb icing, and I used to climb up to several thousand feet, throttle back and decend to see if we had affected a cure after every modification.? The engine only ever stopped on me? in the circuit, never during these tests!? Frequently stopping on the "final glide".? I got to the state where I refused to go around, no matter how bad the landing, as opening the throttle would cause the engine to splutter and die every time.
The final cure was to fit small electric heaters onto the body of the Carb.? I would switch them on before every descent and switch them off for normal flight and this cured the problem for me.? The sump oil carb heat did not work adequately in the UK climate whilst descending.
Another pilot said, subsequent to his accident, that he left the heater turned off "to save the battery" he restarted the engine three times in the circuit after it had stopped, but still failed to turn on the heater. (This same mentality causes drivers to drive on parking lights when in their cars, which makes them virtually invisible after dark.) ? The final stoppage was too low to affect a restart and the crash wrote of the aircraft.
The problem with the carb was finally cured with electric carb heat, but there is no cure for stupidity!
Cheers,
Mo Davies.
.? Justin Gregoris wrote:
Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


Virus-free.


 

开云体育

Get a 912 and in my opinion save yourself a lot of trouble


On 1 May 2022, at 10:36, Mo Davies via groups.io <modavies@...> wrote:

?
Many years ago, we had a series of engine stoppages with an early Jab.? We tried all manner of tricks to prevent carb icing, and I used to climb up to several thousand feet, throttle back and decend to see if we had affected a cure after every modification.? The engine only ever stopped on me? in the circuit, never during these tests!? Frequently stopping on the "final glide".? I got to the state where I refused to go around, no matter how bad the landing, as opening the throttle would cause the engine to splutter and die every time.
The final cure was to fit small electric heaters onto the body of the Carb.? I would switch them on before every descent and switch them off for normal flight and this cured the problem for me.? The sump oil carb heat did not work adequately in the UK climate whilst descending.
Another pilot said, subsequent to his accident, that he left the heater turned off "to save the battery" he restarted the engine three times in the circuit after it had stopped, but still failed to turn on the heater. (This same mentality causes drivers to drive on parking lights when in their cars, which makes them virtually invisible after dark.) ? The final stoppage was too low to affect a restart and the crash wrote of the aircraft.
The problem with the carb was finally cured with electric carb heat, but there is no cure for stupidity!
Cheers,
Mo Davies.
.? Justin Gregoris wrote:
Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


Virus-free.


 

开云体育

Could the transponder 3amp circuit breaker tripping and then my master 15amp circuit breaker tripping be due to a different battery than what my X Air had?

Previous battery: Odyssey PC680:
Specifications
Pulse (5-second) Hot Cranking Amps (PHCA): 520
Cold Cranking Amps (CCA): 170
20Hr Nominal Capacity (Ah): 16
Reserve Capacity Minutes: 24
Dimensions L x W x H (in): 7.15 x 3.00 x 6.65
Weight (lbs): 15.4

New battery: aerovoltz AI Series 360CCA:

Negative Terminal Location: DUAL
Weight: (2.6 lbs.)
Voltage (Charged): 13.6V
Lead Acid Equivalent Amperage: 6.9 A/H @ 10 A/H Rating
Pulse Cranking Amps: 360amps
Operating Environment: -18°C (0°F) to 60°C (140°F)

I purchased this new battery because how light it is and it says it's good for the Jabiru right on their website.

The only major difference between the old battery and this new one is amp hours from 16AH to 6.1AH.

Could that have caused the main 15amp breaker to trip?


From: [email protected] <[email protected]> on behalf of Brian Ellis via groups.io <bellis2uk@...>
Sent: Sunday, May 1, 2022 5:53:47 AM
To: [email protected] <[email protected]>
Subject: Re: [XAIR] X Air Hanuman: engine-out
?
Get a 912 and in my opinion save yourself a lot of trouble


On 1 May 2022, at 10:36, Mo Davies via groups.io <modavies@...> wrote:

?
Many years ago, we had a series of engine stoppages with an early Jab.? We tried all manner of tricks to prevent carb icing, and I used to climb up to several thousand feet, throttle back and decend to see if we had affected a cure after every modification.? The engine only ever stopped on me? in the circuit, never during these tests!? Frequently stopping on the "final glide".? I got to the state where I refused to go around, no matter how bad the landing, as opening the throttle would cause the engine to splutter and die every time.
The final cure was to fit small electric heaters onto the body of the Carb.? I would switch them on before every descent and switch them off for normal flight and this cured the problem for me.? The sump oil carb heat did not work adequately in the UK climate whilst descending.
Another pilot said, subsequent to his accident, that he left the heater turned off "to save the battery" he restarted the engine three times in the circuit after it had stopped, but still failed to turn on the heater. (This same mentality causes drivers to drive on parking lights when in their cars, which makes them virtually invisible after dark.) ? The final stoppage was too low to affect a restart and the crash wrote of the aircraft.
The problem with the carb was finally cured with electric carb heat, but there is no cure for stupidity!
Cheers,
Mo Davies.
.? Justin Gregoris wrote:
Good afternoon Gents

Background: Jabiru 2200 Bing carburetor was fully serviced for the first time in 14 years by Rotax dealer; also who was my flight instructor who taught me how to fly.

Since the carburetor was off, I decided to route new fuel lines since I did not have a bypass line with a one-way check valve. I also replaced my fuel pump with a brand new fuel pump with a built-in check valve.

Yesterday, I put fresh fuel in and started up the motor for about 10 or 12 minutes and then did a static run test. I went full power for about 10 seconds and then slam their throttle right down to idle to see if it would stall. It did not install. I did this multiple times on the ground.

Today, I fired up the engine and warmed it up as usual and then did a static run before my first flight of the year. I was flying with a pilot that has 48 years of flying experience in over 30 aircraft.

The takeoff went great but then the master breaker popped as well as my 3 amp transponder breaker also popping. I don't know why this happened as it never happened before but I pushed back in the master breaker and we continue flying without any issues.

As we were approaching to land my airplane everything was going well. I was coming in a little too fast so as soon as I was over the runway I moved the throttle right back to idle position at which point I flared too early and the airplane ballooned a little bit but nothing crazy. When a lightly kissed the ground and the nose went up the engine all of a sudden installed and the propeller stopped turning. Luckily at that point I was able to land without any hard effects but both of us were extremely shocked the engine stalled. Thank goodness it was literally right at the end. It easily fired back up and then I did another static run and slammed it back to idle and it did not stop.

I am scratching my head as to why it's stalled. It has never ever done this before. I forgot to use electric boost pump when I was landing which may have helped the issue not even happen? Perhaps it was an air bubble or air pocket that was trapped in the brand new fuel line?

I do not have any fuel leaks right now or smell any fuel and all my brand new lines are bone dry.

I think it is coincidental that the master breaker and the transponder breaker popping has nothing to do with the engine stopping. But that has never happened to me either.

yesterday I noticed my engine idling at about 12:00 or 1300 RPM so this morning I took out my 7 mm wrench to try and lower the idle stop screw at which point it did and now it idles at about 1,000 RPM.

Any guidance as to the culprits of the engine stopping is greatly appreciated as I intend to fly in 2 days from now and do not want this to happen again. Thank you
?


Virus-free.


 

...Thought i'd share my experience that I went through today with everyone:

After the mishap (first flight of the year; electrical and mechanical issues) a few days ago, I didn't sleep much, but rather spent the time researching and researching some more.

I still can't fully understand what exactly happened, but today was relieving and exhilarating- 11 take-offs and landings with no issues whatsoever. I removed the new 2lb "intelligent" battery and re-installed the old 16lb battery. I also turned the idle set screw back to its position prior to the Rotax mechanic servicing my Jabiru/Bing carb.

After lots of speculating, here is what I think happened with my electrical circuit breakers tripping both 3A transponder and 15A master: the new battery only puts out 6 amp hours of current, plus it has some 'intelligent' circuitry installed within it, whereby reacting a lot faster to over/under voltage, over/under current, and other situations that may impact both series and parallel circuits within the system. I think it was being too sensitive, plus not enough amp hours, like the old 16 amp hour, 16lb AGM battery. Another potential culprit (although quite rare) may have also contributed to the high frequency sound in my headset as soon as i left ground/earth: I was using a large 4'x4' microfiber towel to clean all the dust off the plane since it is barn hangered throughout the winter. Anytime I use a microfiber towel, the hairs on my arms and hands stand up, so I couldnt only imagine how it may have reactyed to my plane leaving earth/ground reference. I know it may sound farfetched, but you never know; static imoacts electronics more than some may think.

When dealing with my engine shutting off without notice as soon as I touched the ground was not because of an air pocket but rather from the instantaneous impact of landing and its effect on the idle level on the carb. Although I did a static test after lowering the RPM, the Rotax dealer said he has seen time and time again; an even-lower RPM drop after the carb has been subjected to not only a fine-tune adjustment, but also impact/vibration. That is what I believed casued my engine to quit as soon as my wheels 'bounced' off the ground from the first landing of the year / in 5 months of no-flying.

Needless to say, this is a lesson for me. I thought I was saving significant weight with a lithium ion battery, with the inclusion of an extra 150+CCA. I did not however, pay attention to the amp-hour rating as well as any other features a different battery may have from the original battery.

The flight today was a blast and everything was running as it should.

I even swtiched from 100LL to Shell V Power 91 and it runs cleaner, after inspecting the valves; I can notice the lead/carbon residue being disturbed and eventually burned, which is another relief.

The propeller spinner nose cone even reduced the CHT by about 3-4 degrees celcius, which I was also glad to see.


 

开云体育

This is great to hear Justin!

Get


From: [email protected] <[email protected]> on behalf of Justin Gregoris <jgregoris789@...>
Sent: Tuesday, May 3, 2022 11:36:28 AM
To: [email protected] <[email protected]>
Subject: Re: [XAIR] X Air Hanuman: engine-out
?
...Thought i'd share my experience that I went through today with everyone:

After the mishap (first flight of the year; electrical and mechanical issues) a few days ago, I didn't sleep much, but rather spent the time researching and researching some more.

I still can't fully understand what exactly happened, but today was relieving and exhilarating- 11 take-offs and landings with no issues whatsoever. I removed the new 2lb "intelligent" battery and re-installed the old 16lb battery. I also turned the idle set screw back to its position prior to the Rotax mechanic servicing my Jabiru/Bing carb.

After lots of speculating, here is what I think happened with my electrical circuit breakers tripping both 3A transponder and 15A master: the new battery only puts out 6 amp hours of current, plus it has some 'intelligent' circuitry installed within it, whereby reacting a lot faster to over/under voltage, over/under current, and other situations that may impact both series and parallel circuits within the system. I think it was being too sensitive, plus not enough amp hours, like the old 16 amp hour, 16lb AGM battery. Another potential culprit (although quite rare) may have also contributed to the high frequency sound in my headset as soon as i left ground/earth: I was using a large 4'x4' microfiber towel to clean all the dust off the plane since it is barn hangered throughout the winter. Anytime I use a microfiber towel, the hairs on my arms and hands stand up, so I couldnt only imagine how it may have reactyed to my plane leaving earth/ground reference. I know it may sound farfetched, but you never know; static imoacts electronics more than some may think.

When dealing with my engine shutting off without notice as soon as I touched the ground was not because of an air pocket but rather from the instantaneous impact of landing and its effect on the idle level on the carb. Although I did a static test after lowering the RPM, the Rotax dealer said he has seen time and time again; an even-lower RPM drop after the carb has been subjected to not only a fine-tune adjustment, but also impact/vibration. That is what I believed casued my engine to quit as soon as my wheels 'bounced' off the ground from the first landing of the year / in 5 months of no-flying.

Needless to say, this is a lesson for me. I thought I was saving significant weight with a lithium ion battery, with the inclusion of an extra 150+CCA. I did not however, pay attention to the amp-hour rating as well as any other features a different battery may have from the original battery.

The flight today was a blast and everything was running as it should.

I even swtiched from 100LL to Shell V Power 91 and it runs cleaner, after inspecting the valves; I can notice the lead/carbon residue being disturbed and eventually burned, which is another relief.

The propeller spinner nose cone even reduced the CHT by about 3-4 degrees celcius, which I was also glad to see.