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Can a PC operate a BOSS 5 or 6? (and a question)
I've been running a Boss 5 from my pc for over a year now. I use
Deskcnc, which seems to do a great job of running the mill, but I don't use it much for programming. I've got gecko 201s and they drive the stock stepper motors pretty well. Now that i've said it can be done, I have a question for everyone else. One problem I've had recently is the Z axis stepper keeps losing steps. I wrote about a month ago and said it was losing power (by the way thanks to all who replied, I don't get on here very often), but a few changes in my acceleration profile, and it seems to run pretty fast again. However all the adjustments I make don't seem to fix the step loss problem. It doesn't lose them all the time either. I'm running a 3d profiling program with about 65,000 lines of code, with the top of the part at Z0, and the bottom at Z-.150. By the end of the program its usually off by about .050" but sometimes as much as .200". Also this motor seems a lot hotter than the Y and X motors, although they are all the same kind of motor. I'm considering changing to servos, but don't have any experience with them. Would I be able to change just the Z axis to a servo and geck0 3whatever, and leave steppers on x and y? I found what looks like a good deal on www.homeshopcnc.com and would like to know if this servo would drive this machine. thanks Nathan Clymer |
Raymond Heckert
Check to make sure that the Z-axis isn't binding up somewhere. Also check
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that the timing belt is 'drum-tight', and free of oil, grease, etc. RayHex -----Original Message-----
Date: Monday, September 04, 2006 4:01 PM Subject: [CAD_CAM_EDM_DRO] Re: Can a PC operate a BOSS 5 or 6? (and a question) <snip> One problem I've had recently is the Z axis stepper keeps losing steps. I wrote about a month ago and said it was losing |
Les Newell
Hi Nathan,
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This a a fairly common problem. After a lot of use the slideway oil tends to leave a gummy deposit where the quill slides in the head. I found that taking the front cover off, cleaning out the oil then pouring in some cellulose (lacquer) thinners and running the quill up and down a few hundred times helped wash out the crap. You can change to a servo on the Z without changing the other axes. That servo you are looking at hasn't really got enough torque to use as drop-in replacement. Ideally you need one with 2.5 - 3x the torque. You can get around the problem by fitting a smaller pulley on the motor but this can be hard work. It is a big job to change the belt. If you do this be very careful to make sure the ball nut does not run off the end of the screw. According to Bridgeport if you do this you have to replace the nut and screw! You may also have to relocate the motor mounting holes if the belt does not line up perfectly. Les rocketscientistnate wrote: Now that i've said it can be done, I have a question for everyone else. One problem I've had recently is the Z axis stepper keeps losing steps. I wrote about a month ago and said it was losing power (by the way thanks to all who replied, I don't get on here very often), but a few changes in my acceleration profile, and it seems to run pretty fast again. However all the adjustments I make don't seem to fix the step loss problem. It doesn't lose them all the time either. I'm running a 3d profiling program with about 65,000 lines of code, with the top of the part at Z0, and the bottom at Z-.150. By the end of the program its usually off by about .050" but sometimes as much as .200". Also this motor seems a lot hotter than the Y and X motors, although they are all the same kind of motor. |
There doesn't appear to be that much gummy stuff, and most of it is
at the end. When the machine is off, I can turn the motor and move the quill quite easily by turning the position indicator (about 1.5" diameter) mounted on the end of the motor shaft. It moves smoothly and easily all the way up and down. Should the stickiness be something I should be able to feel when doing this? It won't hurt it to give it a good cleaning and it sounds like the cheapest potential solution. Also are you saying that all motors for this need about 2500 oz-in of torque? Or that servos need 3 times as much as steppers? I think I had read about 900 oz-in for a stepper replacement works good on these. Thanks Nathan Clymer --- In CAD_CAM_EDM_DRO@..., Les Newell <lesnewell@...> wrote: oil tends to leave a gummy deposit where the quill slides in the head.I found that taking the front cover off, cleaning out the oil thenpouring in some cellulose (lacquer) thinners and running the quill up anddown a few hundred times helped wash out the crap.axes. That servo you are looking at hasn't really got enough torque to use astorque. You can get around the problem by fitting a smaller pulley on themotor but this can be hard work. It is a big job to change the belt. If youdo this be very careful to make sure the ball nut does not run offthe end of the screw. According to Bridgeport if you do this you have toreplace the nut and screw! You may also have to relocate the motormounting holes if the belt does not line up perfectly. |
Les Newell wrote:
Hi Nathan,My method of freeing a Bridgeport quill that was binding was to extend it fully and wipe axle grease all over the quill, then retract and work in and out a few times, then extend fully again. Wipe off the grease PLUS all the grit, chips, etc. that have stuck to the grease, then repeat. When the grease comes off the quill without little sparkly bits in it, then you can wipe it off and relube with oil. Before the purists jump all over me, this is for a quill that is BADLY contaminated and full of score marks. Don't do this on a shiny and smooth Bridgeport quill, or you may bind it up even worse. I had to beat the quill out of my head casting with a large wood block and a sledge hammer. It had been fully retracted and left in a garage for 15 - 20 years. It is a tribute to Bridgeport's fine machining that it still works fine after all that. I got LOTS of chips out of the space between the quill and housing. I assume it was all packed into the score marks, as the quill is still a VERY snug fit. Jon |
rocketscientistnate wrote:
There doesn't appear to be that much gummy stuff, and most of it is at the end. When the machine is off, I can turn the motor and move the quill quite easily by turning the position indicator (about 1.5" diameter) mounted on the end of the motor shaft. It moves smoothly and easily all the way up and down. Should the stickiness be something I should be able to feel when doing this?Yes, if it is binding, then you would be able to feel it. It won't hurt it to give it a good cleaning and it sounds like the cheapest potential solution. Also are you saying that all motors for this need about 2500 oz-in of torque? Or that servos need 3 times as much as steppers? I think I had read about 900 oz-in for a stepper replacement works good on these.No, 2500 Oz-In would break things. Usually, because steppers lose so much of their (holding) torque when moving, a servo with a much lower rating can be used. I'm using a motor with about 150 Oz-In torque on my Bridgeport quill. This isn't a BOSS quill, but a manual head with an external ballscrew added to the front. The Bridgeport power feed has an overload clutch that is to be set at 200 Lbs. linear force, so you don't want more than that, anyway. So, I'm suspecting there is some other problem that is causing lost steps. Could a pulley be loose and slipping? I've sure seen this before. Make sure the lube system is getting to the quill ballscrew, the lines or metering orifices can clog up. Jon |
Les Newell
If you can easily move the quill up and down you probably don't have a problem. Most commercial retrofits use around 400 - 500 oz-in continuous torque rated motors. Those motors are 170 oz-in continuous.
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Les rocketscientistnate wrote: There doesn't appear to be that much gummy stuff, and most of it is at the end. When the machine is off, I can turn the motor and move the quill quite easily by turning the position indicator (about 1.5" diameter) mounted on the end of the motor shaft. It moves smoothly and easily all the way up and down. Should the stickiness be something I should be able to feel when doing this? It won't hurt it to give it a good cleaning and it sounds like the cheapest potential solution. Also are you saying that all motors for this need about 2500 oz-in of torque? Or that servos need 3 times as much as steppers? I think I had read about 900 oz-in for a stepper replacement works good on these. |
No, 2500 Oz-In would break things. Usually, because steppers loseso much ofrating can be used. I'm using a motor with about 150 Oz-In torque on myBridgeport quill. This isn't a BOSS quill, but a manual head with an externalballscrew added tois to be setlost steps. Could a pulley be loose and slipping? I've sure seen this before.lines or metering I reread the advert at homeshopcnc.com. Its 850 oz-in PEAK. 170 constant. Its definitly not a pulley slipping, I can watch the end of the motor shaft. I wrote a short program to just move the quill up and down, and watched it. It can go up and down a hundred times and then it just kinda stalls on one move and makes a nasty grinding noise but just creeps a little. When the controller sends it the other way, it takes off and goes fine again for a while. If it was something that happened everytime i did something in particular it would be easy to diagnose. I don't know if it helps, but everytime I run a program and it does this, it seems to lose steps in the same direction everytime it does it. Like in this program everytime it loses some it will be higher, or the next time I run it they will always be lower. Or say I'm running a 3d part where the x moves back and forth stepping .005 in the y every pass, (z axis making the profile) the whole part will be tapered from the lower to higher y values at a fairly consistent taper. Sometimes it tapers up, sometimes down, and ocasionally it works fine. If instead it lost steps both directions, it would be rough and jagged, but not consistently tapered. Thanks Nathan |
--- In CAD_CAM_EDM_DRO@..., Les Newell <lesnewell@...>
wrote: have a problem. Most commercial retrofits use around 400 - 500 oz-incontinuous torque rated motors. Those motors are 170 oz-in continuous. I had a spare motor that came with the mill, but I hadn't tested it yet. I got it out, it ran great so I mounted it on the mill. No luck, it does the same thing. I turned the belt and the ballscrew inside the head and it couldn't have been any freeer. (freer? never spelled that before) I'm pretty confident in the deskcnc control board and the gecko drives, unless during the series of short moves (less than .005") they get ahead of the machine, but I don't think that should happen. I'm wondering if running the combination of all three drives is somehow depleting the current to that motor, but I doubt this too. The power supply is just like you (Les) explained to me a couple years ago. 1 transformer, a bridge rectifier (actually three in parallel because they were there) and some capacitors for filters. It seems like it almost has to be in my acceleration curves, but I can't seem to work it out right. Thanks Nathan |
rocketscientistnate wrote:
Hmmm, I wonder if you have a chip in your ballnut? I get these in my machine every once in a while. My marginal quill motor will sometimes stall on this. My EMC software is continuously reading the encoder position, and if it lags more than a little, it will stop on a following error and let me know there is a problem. What good are servos if it just blindly goes on mis-making the part? (This is not a big problem here, it happens once every few years.) My ballscrew is on the front of the quill (a retrofitted manual 1J head) and more prone to crud getting into it. Yours is pretty hard to get to, so my trick with greasing and cleaning may be the only way to get chips out of the ballnut or its roller bearings. Are you using Gecko 320/340 drives? They should fault out when they get behind by 128 steps. I don't know if it helps, but everytime I run a program and it does this, it seems to lose steps in the same direction everytime it does it. Like in this program everytime it loses some it will be higher, or the next time I run it they will always be lower. Or say I'm running a 3d part where the x moves back and forth stepping .005 in the y every pass, (z axis making the profile) the whole part will be tapered from the lower to higher y values at a fairly consistent taper. Sometimes it tapers up, sometimes down, and ocasionally it works fine. If instead it lost steps both directions, it would be rough and jagged, but not consistently tapered.This makes me think it might be an acceleration problem, or possibly something to do with the timing between step pulses and changes in the direction signal. Jon |
I have problem with Z steps on my micro mill.
After rechecking and testing everything electrical and mechanical, found that problem was with backslash compensation(I'm using TurboCNC). I put zero there and no lost steps on Z anymore. Leo --- In CAD_CAM_EDM_DRO@..., "Raymond Heckert" <jnr@...> wrote: check that the timing belt is 'drum-tight', and free of oil, grease, etc. |
Les Newell
I had exactly the same problems as you. On top of lost steps I had problems with the Z drive blowing. In the end I changed over to servos and now it performs brilliantly. Rapids are limited to about 100IPM because I used undersized motors and geared them down. However that is more than enough for what I do.
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Les rocketscientistnate wrote: I had a spare motor that came with the mill, but I hadn't tested it yet. I got it out, it ran great so I mounted it on the mill. No luck, it does the same thing. I turned the belt and the ballscrew inside the head and it couldn't have been any freeer. (freer? never spelled that before) I'm pretty confident in the deskcnc control board and the gecko drives, unless during the series of short moves (less than .005") they get ahead of the machine, but I don't think that should happen. I'm wondering if running the combination of all three drives is somehow depleting the current to that motor, but I doubt this too. The power supply is just like you (Les) explained to me a couple years ago. 1 transformer, a bridge rectifier (actually three in parallel because they were there) and some capacitors for filters. It seems like it almost has to be in my acceleration curves, but I can't seem to work it out right. |
--- In CAD_CAM_EDM_DRO@..., Les Newell <lesnewell@...>
wrote: servos and now it performs brilliantly. Rapids are limited to about100IPM because I used undersized motors and geared them down. Howeverthat is more than enough for what I do. I would love to do that. Where is the best place to get the servos? What size do I need, to gear them down and go undersize, or to go 1:1. I assume I'll need gecko 320s? What are the possible hang ups in doing this? With the encoders is it pretty much guaranteed that if its running the servos are going to be in the right place? I'm a little anxious as I have customers starting to breath down my neck. Luckily, the local college lets me use their Fadal when I'm broken down. :) I had almost decided to try to sell the whole machine and get a smaller benchtop one, that I could be sure would work. I thought if I go to servos, its my luck that it still won't work and then I'll have the same useless machine, and still be out the money for servos. Thanks Nathan |
Les Newell
Hi Nathan,
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I went the cheapskate route and bought some treadmill motors from Surplus Center. They were similar to these: <>. Mine have a short shaft sticking out the back, perfect for an encoder. You would have to ask to find out if these motors also have a shaft sticking out the back. Surprisingly for a cheap motor they run very smoothly at low speed. The only problem is that they are designed for high revs so you need to gear them down at least 3:1 to work well. My Z axis is about 2:1 if I remember correctly and the motor can get a bit hot if you keep running the Z up and down at rapid speed for a while. In actual use none of the motors get particularly hot. To get a suitable ratio you need to use different belts. I used 15mm HTD belts on X and Y. You can't easily change the Z axis pulley which is why I couldn't get the ratio I wanted. Be warned belts and pulleys can be expensive! If you are using the machine for work it is probably not worth spending the effort and time to use these motors. You would be better off finding a more suitable motor even if it is more expensive. As I mentioned before you need somewhere around 30 lb-in (480oz-in) continuous rated torque if you want to re-use the existing pulleys. As long as you are reasonably careful about screening and use good quality cable on the encoders you are unlikely to lose steps. That is what I really like about my servo setup. I don't have to worry that a stepper may have lost steps somewhere along the line. I use Gecko G320s on the mill and Rutex R990H on my lathe. IMHO the R990s give very slightly better performance but they are more hassle to wire up. Don't sell your Bridgeport. No benchtop machine will compete with it once you have it working correctly. Les rocketscientistnate wrote: I would love to do that. Where is the best place to get the servos? What size do I need, to gear them down and go undersize, or to go 1:1. I assume I'll need gecko 320s? What are the possible hang ups in doing this? With the encoders is it pretty much guaranteed that if its running the servos are going to be in the right place? I'm a little anxious as I have customers starting to breath down my neck. Luckily, the local college lets me use their Fadal when I'm broken down. :) I had almost decided to try to sell the whole machine and get a smaller benchtop one, that I could be sure would work. I thought if I go to servos, its my luck that it still won't work and then I'll have the same useless machine, and still be out the money for servos. |
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